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Old 09-15-2015, 12:15 AM   #2004 (permalink)
thingstodo
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Join Date: Sep 2010
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Update for Sep 14

Took the DC and AC controllers off the mounting plate (separated Cougar controller), remove the mounting plate - was mounted over both motors

Move the AC controller (still connected to the AC motor)

Remove the motor supports (most of them)

Decouple the motors

Pack up for the night

- located some of the parts required to make a small circuit board out of the voltage divider network for the encoder

- it does not appear that the netgain warp 9 can reliably withstand a 10,000 rpm test. So I decoupled the DC motor and now need to get the encoder coupled to the motor directly .. after I figure out where to put the DC motor for a few days.
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Last edited by thingstodo; 09-15-2015 at 12:18 AM.. Reason: rpm rating
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MPaulHolmes (09-15-2015)